18 troubleshooting, 1 troubleshooting guide, Troubleshooting – Flowserve 500+ Series Logix User Manual

Page 50: Roubleshooting, Uide

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User Instructions - Logix® 500+ Series Digital Positioners FCD LGENIM0105-10 11/13

flowserve.com

50


18 TROUBLESHOOTING

18.1 Troubleshooting Guide


Table 25: Troubleshooting Guide

Failure

Probable Cause

Corrective action

No LED is blinking.

1. Current source too low.
2. Voltage of current source is too low.
3. Incorrect wiring polarity.

1. Verify current source supplies at least 3,8 mA.
2. Verify voltage source supplies at least 10VDC.
3. Check wiring for correct polarity.

Erratic communications.

1. Current source bandwidth not

limited to 25Hz.

2. Maximum cable length or cable

impedance exceeded.

3. HART modem connected to PC RS-

232 port not receiving enough power

4. Interference with I.S. barrier.
5. Current source stripping (filtering)

HART signal.

1. Maximum allowable current source rate of change is

924 mA per second.

2. Check cable size, length and capacitance. See

Section 7 ELECTRICAL CONNECTIONS.

3. Verify laptop battery is not low.
4. Must use HART compatible I.S. barrier.
5. Use a

250Ω resistor and a 22 µF capacitor to create

a HART filter according to the following schematic.

Unit does not respond
to analog commands.

1. The positioner is in digital

command mode.

2. An error occurred during

calibration.

1. Switch to analog command mode using the

procedure outlined in Section 9.3 Command
Source Reset,
use the ValveSight DTM, or
use a handheld communicator.

2. Check Status Codes. Correct calibration

error. Recalibrate.

Valve position reading
is not what is
expected.

1. Stem position sensor mounting

is off 180 degrees.

2. Stroke not calibrated
3. Tight shutoff MPC (Minimum

position cutoff) is active.

4. Custom characterization or soft

stops are active.

1. Reposition the sensor.
2. Perform a Stroke calibration (Quick-Cal).
3. Verify Tight Shutoff settings.
4. Verify custom characterization or soft-stop limits.

Position is driven fully
open or closed and will
not respond to
command.

1. Stroke is not calibrated.
2. Inner-loop hall sensor is not

connected.

3. Wrong air action was entered in

software.

4. Actuator tubing is backward.
5. Electro-pneumatic

converter is
malfunctioning.

6. Control parameter inner-loop

offset is too high/low.

1. Perform stroke calibration (Quick-Cal)
2. Verify hardware connections.
3. Check ATO (Air-to-open) and ATC (Air-to-Close)

settings. Recalibrate using Quick-Cal to apply
settings.

4. Verify ATO/ATC actuator tubing.
5. Replace electro-pneumatic converter.
6. Adjust inner-loop and see if proper control

resumes.

Sticking or hunting
operation of the positioner

1. Contamination of the electro-

pneumatic converter.

2. Control tuning parameters not

correct.

3. Packing friction is high.

4. Spool valve is corroded or dirty.

1. Check air supply for proper filtering and meeting

ISA specifications ISA-7.0.01.

2. Lower proportional gain settings.
3. Enable the stability DIP switch on the local

interface and recalibrate. If problem persists,
adjust pressure control window with handheld
communicator or ValveSight and recalibrate.

4. Disassemble and clean spool valve.

LCD backlight flickering or
dim.

1. The backlight uses any residual

power not used by other functions of
the circuitry.

1. Fluctuations in the LCD backlight are normal. No

action required.

22 µF 250Ω

Control System

HART
Comm
Device

To Logix

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