Flowserve 510si IOM Logix User Manual

Page 13

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13

Colors Identifier

Indication and resolution

Y - - -

Any sequence starting with a yellow light indicates that the unit is in a special calibration or test mode, or that
there was a calibration problem.

YYYR

4

Command minimum saturated - Calibration error indicating that the 4-20 mA signal corresponding to the
minimum command was too low. Adjust the signal to higher range and re-do the calibration. This error may
be cleared by briefly pushing the quick-cal button, which will force the positioner to use the parameters from
the last good calibration.

YYRR

5

Command span - Calibration error indicating that the 4-20 mA signal was below the minimum calibration span.
The minimum calibration span is 3.0 mA. This error may be cleared by briefly pushing the quick-cal button,
which will force the positioner to use the parameters from the last good calibration or if the ∆ and ∇ buttons
are pressed simultaneously the calibrated span will be used even though it is less than the recommended range.

YYRY

6

Command maximum saturated - Calibration error indicating that the 4-20 mA signal corresponding the
maximum command was too high. Adjust the signal a lower range and re-do the calibration. This error may
be cleared by briefly pushing the quick-cal button, which will force the positioner to use the parameters from
the last good calibration.

YYGG

7

Calibration complete - Indicates that a 4-20 command calibration is complete. This pause allows the signal to be adjusted
without affecting the valve position. Press the ∆ and ∇ buttons simultaneously to put the unit back in operation.

YRRR

8

Feedback span - The range of motion of the position feedback arm was too small. Check for loose linkages
and/or adjust the feedback pin to a position closer to the follower arm pivot to create a larger angle of rotation.
Also check the air supply to make sure the system is properly connected. This error may be cleared by briefly
pushing the quick-cal button, which will force the positioner to use the parameters from the last good
calibration or if the ∆ and ∇ buttons are pressed simultaneously the calibrated span will be used even though
it is less than the recommended range.

YRRY

9

Feedback 100 saturated - Calibration error indicating that the position sensor was out of range during the
calibration. To correct the condition, adjust the positioner mounting, linkage or feedback potentiometer to
move the position sensor back into range then restart the calibration. This error may be cleared by briefly
pushing the quick-cal button, which will force the positioner to use the parameters from the last good calibration.

YRRG

10

Waiting for 100% position JOG set point from User - only used during Jog calibration see explanation in
Quick-Cal section of main document for operation.

YRYY

11

Feedback no-motion during calibration - Indicates that there was no motion of the actuator based on the
current stroke time configuration. Check linkages and air supply to make sure the system is properly
connected. If the time out occurred because the actuator is very large then simply retry the Quick cal and the
positioner will automatically adjust for a larger actuator by doubling the time allowed for movement. This error
may be cleared by briefly pushing the quick-cal button, which will force the positioner to use the parameters
from the last good calibration.

YRYG

12

Setting IL offset (during Stroke calibration) - An automatic step in the calibration process that is done with
the valve a 50% position. This must be completed for proper operation.

YRYR

13

Feedback 0 saturated - Calibration error indicating that the position sensor was out of range during the
calibration. To correct the condition, adjust the positioner mounting, linkage or feedback potentiometer to
move the position sensor back into range then restart the calibration. This error may be cleared by briefly
pushing the quick-cal button, which will force the positioner to use the parameters from the last good calibration.

YRGG

14

Stroke Calibration in Progress - Calibration sequence started using the local Quick- Cal button. It may be
cancelled by briefly pushing the quick-cal button.

YRGY

15

Unable to set IL offset during QUICK-CAL – This may occur on very large or small actuators on the first
calibration attempt. The Logix 510 will automatically adjust parameters for future calibrations. To Continue
briefly push the quick-cal button to acknowledge and restart Quick-Cal.

YRGR

16

Feedback unstable during calibration - Check for loose linkages or loose positioner sensor. This error may
be cleared by briefly pushing the quick-cal button, which will force the positioner to use the parameters from
the last good calibration.

YGGG

17

4-20 mA output O% - Waiting for the user to adjust the 0% 4-20 mA output during calibration.

YGGY

18

4-20 mA input O% - Waiting for 0% 4-20 mA command input during command calibration.

YGGR

19

Jog O% - Waiting for 0% position JOG set point from User - only used during Jog calibration see explanation
in Quick-Cal section of main document for operation

YGYY

20

4-20 mA output 10O% - Waiting for the user to adjust the 100% 4-20 mA output during calibration.

YGYR

21

4-20 mA input 10O% - Waiting for 100% 4-20 mA command input during command calibration.

YGRY

22

Analog output span too small - The span must be calibrated to a range greater than 3.0 mA. This error may
be cleared by briefly pushing the quick-cal button, which will force the positioner to use the parameters from
the last good calibration or if the ∆ and ∇ buttons are pressed simultaneously the calibrated span will be used
even though it is less than the recommended range.

YGRR

23

JOG Control Mode - the unit has been placed in a local override mode where the valve can only be stroked using
the two local jog buttons. It may be cancelled by briefly pushing the quick-cal button.

Logix 510si Status Condition Codes

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