English-20 – Rockwell Automation 25D PowerFlex 40P Quick Start - FRN 1.xx - 3.xx User Manual

Page 20

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English-20

F6

Motor Stalled

(1)

Increase [Accel Time x] or reduce load so drive output current does not exceed the current set
by parameter A089 [Current Limit].

F7

Motor Overload

(1)

An excessive motor load exists. Reduce load so drive output current does not exceed the
current set by parameter P033 [Motor OL Current]. Verify A084 [Boost Select] setting.

F8

Heatsink OvrTmp

(1)

Check for blocked or dirty heat sink fins. Verify that ambient temperature has not exceeded
40

°

C (104

°

F) for IP 30/NEMA 1/UL Type 1 installations or 50°C (122°F) for Open type installations.

Check fan.

F12

HW OverCurrent

Check programming. Check for excess load, improper DC boost setting, DC brake volts set too
high or other causes of excess current.

F13

Ground Fault

Check the motor and external wiring to the drive output terminals for a grounded condition.

F29

Analog Input Loss

(1)

An analog input is configured to fault on signal loss. A signal loss has occurred.
Check parameters. Check for broken/loose connections at inputs.

F33

Auto Rstrt Tries

Correct the cause of the fault and manually clear.

F38

Phase U to Gnd

Check the wiring between the drive and motor.
Check motor for grounded phase.
Replace drive if fault cannot be cleared.

F39

Phase V to Gnd

F40

Phase W to Gnd

F41

Phase UV Short

Check the motor and drive output terminal wiring for a shorted condition.
Replace drive if fault cannot be cleared.

F42

Phase UW Short

F43

Phase VW Short

F48

Params Defaulted

The drive was commanded to write default values to EEPROM.
Clear the fault or cycle power to the drive. Program the drive parameters as needed.

F63

SW OverCurrent

(1)

Check load requirements and A098 [SW Current Trip] setting.

F64

Drive Overload

Reduce load or extend Accel Time.

F70

Power Unit

Cycle power. Replace drive if fault cannot be cleared.

F71

Net Loss

The communication network has faulted.
Cycle power. Check communications cabling.
Check network adapter setting. Check external network status.

F80

SVC Autotune

The autotune function was either cancelled by the user of failed. Restart procedure.

F81

Comm Loss

If adapter was not intentionally disconnected, check wiring to the port. Replace wiring, port
expander, adapters or complete drive as required.
Check connection.
An adapter was intentionally disconnected. Turn off using A105 [Comm Loss Action].
Connecting I/O Terminal 04 to ground may improve noise immunity.

F91

Encoder Loss

Requires differential encoder. One of the 2 encoder channel signals is missing.
Check Wiring.
If P038 [Speed Reference] = 9 “Positioning” and E216 [Motor Fdbk Type] = 5 “Quad Check”
swap the Encoder channel inputs (see page 13) or swap any two motor leads.
Replace encoder.

F100 Parameter Checksum Restore factory defaults.
F111 Enable Hardware

DriveGuard Safe-Off Option (Series B) board is installed and the ENBL enable jumper has not
been removed.
Remove the ENBL enable jumper. Cycle power.
DriveGuard Safe-Off Option (Series B) board has failed.
Remove power to the drive. Replace DriveGuard Safe-Off Option (Series B) board.
Hardware Enable circuitry has failed.
Replace drive.

F122 I/O Board Fail

Cycle power. Replace drive if fault cannot be cleared.

(1)

Auto-Reset/Run type fault. Configure with parameters A092 and A093.

No.

Fault

Description

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