LINK Systems Omni II Automatic Setups Module User Manual

Page 60

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October 16, 2008

Manual Version 1.1

6-6

Auto-Move Active

The

slide

is

automatically

going

to the programmed slide setpoint.


Ext Jog Up

The optional external jog up button is active. The slide should be
moving up.

Ext Jog Down

The optional external jog down button is active. The slide should be
moving down.

Section 6.6

Slide Adjust Messages Calibration Only


OK

The slide adjust system calibration results are okay.


Upper Cal Pos MUST be GREATER than Lower
Cal Pos

The numeric value for the upper calibration position must be larger
than the numeric value for the lower calibration position.

Rotary Fine1 Read Failed

The rotary transducer value read from the fine resolver is invalid. This

could be caused by a bad connection, a bad rotary transducer, or a
hardware problem on the rotary circuit board (5100-10C).


Rotary Coarse Read Failed The rotary transducer value read from the coarse resolver is invalid.

This could be caused by a bad connection, a bad rotary transducer, or a
hardware problem on the rotary circuit board (5100-10C).


Rotary Fine2 Read Failed The rotary transducer value read from the fine resolver is invalid. This

could be caused by a bad connection, a bad rotary transducer, or a
hardware problem on the rotary circuit board (5100-10C).


Rotary Fine Reading Drifted The two values read from the fine resolver indicate that the rotary

transducer may have moved at a calibration point. This could be
caused by a bad connection or some unexpected movement at the
rotary transducer.


Rotary Max Turns Exceeded The rotary transducer has exceeded the maximum number of

revolutions. It may be necessary to gear down the input shaft of the
rotary transducer.


Rotary Inc Turn Count Bad The incremental turn count stored in memory has been corrupted.

This usually indicates a problem with the memory device on the main
circuit board (5100-10).


Rotary Quad Read Bad The quadrant of the current resolver reading does not match the

expected value. This could be caused by a bad connection or a
hardware problem on the rotary circuit board (5100-10C).


Resolver Misaligned

The fine and course resolvers are no longer in proper alignment. The
rotary transducer may need to be checked or replaced.

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