Troubleshooting – MITSUBISHI ELECTRIC MELSERVO MR-J2S- A User Manual

Page 203

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10. TROUBLESHOOTING

Display

Name

Definition

Cause

Action

1. Short occurred in servo amplifier

output phases U, V and W.

Correct the wiring.

AL.32

Overcurrent

Current that flew is
higher than the
permissible current
of the servo
amplifier.

2. Transistor (IPM) of the servo

amplifier faulty.

Checking method

Alarm (AL.32) occurs if power is
switched on after U,V and W
are disconnected.

Change the servo amplifier.

3. Ground fault occurred in servo

amplifier output phases U, V and
W.

Correct the wiring.

4. External noise caused the

overcurrent detection circuit to
misoperate.

Take noise suppression measures.

Current higher than
the permissible
current flew in the
regenerative brake
transistor.
(MR-J2S-500A only)

5. Improper wiring of the

regenerative brake option.

Wire the regenerative brake option
correctly.

1. Regenerative brake option is not

used.

Use the regenerative brake option.

2. Though the regenerative brake

option is used, the parameter No.
0 setting is " 00 (not used)".

Make correct setting.

3. Lead of built-in regenerative brake

resistor or regenerative brake
option is open or disconnected.

1. Change lead.
2. Connect correctly.

4. Regenerative transistor faulty.

Change servo amplifier

5. Wire breakage of built-in

regenerative brake resistor or
regenerative brake option

1. For wire breakage of built-in

regenerative brake resistor, change
servo amplifier.

2. For wire breakage of regenerative brake

option, change regenerative brake
option.

6. Capacity of built-in regenerative

brake resistor or regenerative
brake option is insufficient.

Add regenerative brake option or increase
capacity.

7. Power supply voltage high.

Review the power supply.

AL.33

Overvoltage

Converter bus
voltage exceeded
400VDC.

8. Ground fault occurred in servo

amplifier output phases U, V and
W.

Correct the wiring.

1. Pulse frequency of the command

pulse is too high.

Change the command pulse frequency to a
proper value.

2. Noise entered command pulses.

Take action against noise.

AL.35

Command
pulse frequency
error

Input pulse
frequency of the
command pulse is
too high.

3. Command device failure

Change the command device.

1. Servo amplifier fault caused the

parameter setting to be rewritten.

Change the servo amplifier.

2. Regenerative brake option not

used with servo amplifier was
selected in parameter No.0.

Set parameter No.0 correctly.

3. The number of write times to EEP-

ROM exceeded 100,000 due to
parameter write, etc.

Change the servo amplifier.

4.The alarm code output (parameter

No. 49) was set by the absolute
position detection system.

The absolute position detection system
and the alarm code output function are
exclusive. Set as either one of the two is
used.

AL.37

Parameter
error

Parameter setting is
wrong.

5.The alarm code output (parameter

No.49) was set with the
electromagnetic brake interlock
(MBR) assigned to pin CN1B-19.

The signal assignment function of the
electromagnetic interlock (MBR) to pin
CN1B-19 and the alarm code output
function are exclusive. Set as either one of
the two is used.

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