Diagnostics, 4 faults, 1 fault codes – Lenze E94P PositionServo with MVOB User Manual

Page 97

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S94H201E_13426446_EN

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95

Diagnostics

8.4 Faults

8.4.1

Fault Codes

Faults in the drive are immediately shown on the drive display. The fault condition is also recorded to the
drive trip log and the DFaults register inside the drive. The various trip conditions, as they appear on the
display of the drive are listed in the table below.

Fault Codes as Displayed on the Drive

Fault Code

(Display)

Fault

Description

F_OU

Over voltage

Drive bus voltage reached the maximum level, typically due to motor regeneration

F_FB

Feedback error

Invalid Hall sensors code (DFAULT = 2); or Resolver signal lost (DFAULT = 11).

F_OC

Over current

Drive exceeded peak current limit. Software incapable of regulating current within 15%

for more than 20mS. Usually results in wrong motor data or poor tuning.

F_Ot

Over temperature

Drive heatsink temperature has reached maximum rating.

Trip Point = 100°C for all drives except 480V 6A & 9A drives

Trip Point = 108°C for 480V 6A & 9A drives

F_EF

ISO13849-1 fault

The drive is disabled by the ISO13849-1 Safety Function

F_OS

Over speed

Motor has reached velocity above its specified limit

F_PE

Position Error Excess

Position error has exceeded maximum value.

F_bd

Bad motor data

Motor profile data is invalid or no motor is selected.

F_EP

EPM failure

EPM failure on power up

-EP-

EPM missing

EPM not recognized (connected) on power up

F_09

Motor over temperature

Motor over temperature switch activated; Optional motor temperature sensor (PTC)

indicates that the motor windings have reached maximum temperature

F_10

Subprocessor failure

Error in data exchange between processors. Usually occurs when EMI level is high due to

poor shielding and grounding.

F_13

Current feedback error

Current sensor offset is too big (usually noise related).

F_14

Under voltage

(Applies to drive’s with hardware version 1). Occurs when the bus voltage level drops

below 50% of nominal bus voltage while drive is operating. An attempt to enable the drive

with low bus voltage will also result in this fault.

F_15

Hardware overload

protection

Occurs when the phase current becomes higher than 400% of total drive’s current

capability for more then 5

ms.

F_16

Internal Error

Associated with noise. Troubleshoot grounding. If error persists contact factory for

technical support.

F_17

Internal Error

Associated with noise. Troubleshoot grounding. If error persists contact factory for

technical support.

F_18

Arithmetic Error
Division by zero

Statement executed within the Indexer Program results in a division by 0 being

performed. Drive programming error (error in drive source code).

F_19

Arithmetic Error

Register overflow

Statement executed within the Indexer Program results in a value being generated that

is too big to be stored in the requested register. Drive programming error (error in drive

source code).

F_20

Subroutine stack

overflow

Exceeded 32 levels subroutines stack depth. Caused by executing excessive subroutine

calls without a RETURN statement. Drive programming error (error in drive source code).

F_21

Subroutine stack

underflow

Executing RETURN statement without preceding call to subroutine. Drive programming error

(error in drive source code).

F_22

Arithmetic stack

overflow

Variable evaluation stack overflow. Expression too complicated for compiler to process.

Drive programming error (error in drive source code).

F_23

Motion Queue overflow

32 levels depth exceeded. Drive programming error (in drive source code).

F_24

Motion Queue underflow

Relates to the MDV statements in the Indexer Program. Drive programming error (error in

drive source code).

F_25

Unknown

opcode

Byte code interpreter error; May occur when program is missing the closing END

statement; when subroutine has no RETURN statement; or if data in EPM is corrupted at

run-time

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