IAI America SCON-CA User Manual

Page 251

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Chapter 9

Troubleshooting

241

9.2.2 Positioning and speed of poor precision (incorrect operation)

Situation

Possible cause

Check/Treatment

Completion of operation

on the way to home

return

In the home return of our standard

specification, the actuator is first

pressed to the mechanical end,

moved oppositely, and subject to

positioning stop at the home

position. Therefore, the product may

judge as the mechanical end even

though it is still on the way when the

load is large and interfere with

surrounding object.

1) A load exceeding its rating

weight is installed on the

actuator.

2) It is touched to interference in

the way of the run.

3) Torsion stress is applied to guide

due to improper fixing method of

the actuator or uneven fastening

of bolts.

4) The sliding resistance of the

actuator itself is large.

1) Reduce the load.

2) Remove the interference.

3) Loosen the fixing bolts once and

check whether the slider can move

smoothly.

If the slider can move smoothly,

check if there is a deformation on the

attached surface, and install the

actuator again following the

instructions stated in Instruction

Manual.

4) Please contact IAI.

Shocks at start and/or

stop.

Acceleration/deceleration is set too

high.

Decrease the settings of

acceleration/deceleration.

Overshoot during

deceleration to stop.

The load inertia is large.

Decrease the setting of deceleration.

[Refer to 9.3.]

Positioning of poor

precision
Uneven speed during

movement
Acceleration/deceleration

not smooth (bad speed

response)
Trace of poop precision

[Refer to 8.3 Servo Adjustment.]

(Note) When the pulse-train operation mode is selected, first adjust

pulse-train commands.

[In the case of Positioner Mode]

Situation

Possible cause

Check/Treatment

Positioning at a position

different from that of

commanded position No.

PIO signal processing is incorrect.

1) Start signal CSTR is input too

early after position No.

command. Or position No.

command and start signal are

input concurrently.

2) The correct position No. is not

specified due to PIO signal

disconnection or poor connector

contact.

1) The stop position may be set for

another purpose. Input the start

signal after the controller fully reads

the position number.

[Refer to 3.2.4 Operation with the

Position No. Input = Operations of

PIO Patterns 0 to 3. Creating

Sequence Program.]

2) Check the input signal on I/O

monitor on the teaching tool.

Complete signal PEND

is not output even

though positioning

process is completed.

PIO signal processing is incorrect.

1) Start signal CSTR is not turned

OFF.

1) Make the start signal CSTR turned

OFF before completing the

positioning process by the turn-off of

positioning complete signal PEND

after starting operation, and so on.

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