Troubleshooting – MITSUBISHI ELECTRIC MR-J2S- A User Manual

Page 206

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10 - 9

10. TROUBLESHOOTING

Display

Name

Definition

Cause

Action

1. Reduced voltage of super capacitor

in encoder

After leaving the alarm occurring for a few
minutes, switch power off, then on again.
Always make home position setting again.

2. Battery voltage low

Absolute position
data in error

3. Battery cable or battery is faulty.

Change the battery.
Always make home position setting again.

AL.25

Absolute
position erase

Power was switched
on for the first time
in the absolute
position detection
system.

4. Super capacitor of the absolute

position encoder is not charged

After leaving the alarm occurring for a few
minutes, switch power off, then on again.
Always make home position setting again.

1. Wrong setting of parameter No. 0 Set correctly.
2. Built-in regenerative resistor or

regenerative option is not
connected.

Connect correctly

3. High-duty operation or continuous

regenerative operation caused the
permissible regenerative power of
the regenerative option to be
exceeded.

Checking method

Call the status display and check
the regenerative load ratio.

1. Reduce the frequency of positioning.
2. Use the regenerative option of larger

capacity.

3. Reduce the load.

4. Power supply voltage is abnormal.

MR-J2S- A:260VAC or more
MR-J2S- A1:135VAC or more

Check the power supply

Permissible
regenerative power
of the built-in
regenerative
resistor or
regenerative option
is exceeded.

5. Built-in regenerative resistor or

regenerative option faulty.

Change the servo amplifier or
regenerative option.

AL.30

Regenerative
error

Regenerative
transistor fault

6. Regenerative transistor faulty.

Checking method

1) The regenerative option has
overheated abnormally.
2) The alarm occurs even after
removal of the built-in
regenerative resistor or
regenerative option.

Change the servo amplifier.

1. Input command pulse frequency

exceeded the permissible
instantaneous speed frequency.

Set command pulses correctly.

2. Small acceleration/deceleration

time constant caused overshoot to
be large.

Increase acceleration/deceleration time
constant.

3. Servo system is instable to cause

overshoot.

1. Re-set servo gain to proper value.
2. If servo gain cannot be set to proper

value.

1) Reduce load inertia moment ratio; or
2) Reexamine acceleration/

deceleration time constant.

4. Electronic gear ratio is large

(parameters No. 3, 4)

Set correctly.

AL.31

Overspeed

Speed has exceeded
the instantaneous
permissible speed.

5. Encoder faulty.

Change the servo motor.

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