7diagnostics & troubleshooting – Lenze E84AVSCx 8400 StateLine C User Manual

Page 54

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7

Diagnostics & troubleshooting

7.6

Maloperation of the drive

54

Lenze · 8400 StateLine · Operating instructions · from Firmware V06.00 · DMS 1.2 EN · 12/2012 · TD05

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Motor consumes too much current

Torque dip in the field weakening range or

motor stalling during operation in the field weakening range

Asynchronous motor with feedback rotates without control and with too low speed

Motor phase (LP1) monitoring does not respond if the motor phases are interrupted

Cause

Remedy

V

min

boost has been selected too high

Correct setting with C00016

V/f base frequency has been selected too low

Correct setting with C00015

Rated motor data (stator resistance, speed, current,

frequency, voltage) and cos ϕ and/or magnetising

inductance is not adapted to the motor data

Execute automatic motor parameter identification with

the C00002/23 device command

- or -

Adjust motor parameters manually:

C00084: Motor stator resistance

C00087: Rated motor speed

C00088: Rated motor current

C00089: Rated motor frequency

C00090: Rated motor voltage

C00091: Motor cosine phi

C00092: Motor magnetising inductance

Cause

Remedy

Motor is overloaded

Check motor load

Motor windings are wired incorrectly

Reverse from star connection to delta connection

V/f reference point is set too high

Correct setting with C00015

Override point of field weakening is set too low

Correct setting with C00080

Cause

Remedy

Motor phases have been interchanged

• Thus the rotating field of the motor is not identical

anymore with the rotating field of the feedback

system.

• Therefore, the drive shows the following behaviour if

V/f characteristic control (C00006 = 7) is performed:

• The motor rotates faster than the speed setpoint by

the value set in C00074.

• After the controller has been enabled, the

controller will not stop if the speed setpoint = 0 or a

quick stop (QSP) occurs.

• Among other things, the final motor current

depends on the value set for the V

min

boost and

may rise up to I

max

which can trigger the "OC5: Ixt

overload" fault message.

Check the phase position of the motor cable

If possible: Operate the motor with deactivated feedback

(C00006 = 6) and check direction of rotation of the motor

Cause

Remedy

Monitoring is not active (C00597 = 0)

Activate monitoring (C00597 = 1)

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