Yaskawa Sigma-5 User Manual: Operation of Digital Operator User Manual

Page 99

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3.2 Operations

3-65

9

head1

3

Utility Function Mode

„

When “Error” Flashes on the Display

„

When An Error Occurs during Calculation of Moment of Inertia

The following table shows the probable causes of errors that may occur during the
calculation of the moment of inertia with the Jcalc set to ON, along with corrective
actions for the errors.

Error

Probable Cause

Corrective Actions

The gain adjustment

was not successfully

completed.

Machine vibration is occur-

ring or the positioning com-

pleted signal (/COIN) is

turning ON and OFF when

the servomotor is stopped.

• Increase the set value for Pn522.

• Change the mode from 2 to 3.

• If machine vibration occurs,

suppress the vibration with the

anti-resonance control adjust-

ment function and the vibration

suppression function.

An error occurred

during the calculation

of the moment of

inertia.

Refer to the following table „ When An Error Occurs during Cal-

culation of Moment of Inertia.

Travel distance setting

error

The travel distance is set to

approximately 0.5 rotation

(0.05 rotation for SGMCS

servomotor) or less, which

is less than the minimum

adjustable travel distance.

Increase the travel distance. It is

recommended to set the number of

motor rotations to around 3.

The positioning

completed signal

(/COIN) did not turn ON

within approximately 10

seconds after

positioning adjustment

was completed.

The positioning completed

width is too narrow or pro-

portional control (P control)

is being used.

• Increase the set value for Pn522.

• Set V_PPI in the Option field to

0.

The moment of inertia

cannot be calculated

when the tuning-less

function was activated.

When the tuning-less func-

tion was activated, Jcalc was

set to OFF so the moment of

inertia was not calculated.

• Turn OFF the tuning-less func-

tion.

• Set Jcalc to ON, so the moment

of inertia will be calculated.

Error

Display

Probable Cause

Corrective Actions

Err1

The SERVOPACK started calculating

the moment of inertia, but the calcula-

tion was not completed.

• Increase the speed loop gain (Pn100).

• Increase the STROKE (travel dis-

tance).

Err2

The moment of inertia fluctuated greatly

and did not converge within 10 tries.

Set the calculation value based on the

machine specifications in Pn103 and

execute the calculation with the Jcalc set

to OFF.

Err3

Low-frequency vibration was detected.

Double the set value of the moment of

inertia calculating start level (Pn324).

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