NORD Drivesystems BU0500 User Manual

Page 144

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SK 500E – Users Manual for Frequency Inverters

144

BU 0500 GB-1013

E011

11.0

Customer interface

Error in analog-digital converter

Internal customer unit (internal data bus) faulty or
damaged by radio radiation (EMC)

Check control terminals connection for short-circuit.

Minimize EMC interference by laying control and
power cables separately.

Earth the devices and shields well.

Pos : 410 /Anleit ungen/6. / 7. Mel dungen z um Betriebsz ust and [BU 0500 / BU 0200]/ St örmel dungen/F ehl er E012 [ SK 5xxE] @ 2\ mod_1361524186547_388. doc x @ 59066 @ @ 1

E012

12.0

External watchdog

The Watchdog function is selected at a digital input and the
impulse at the corresponding digital input is not present for
longer than the time set in parameter P460 >Watchdog
time<.

Check connections

Check P460 setting

12.1

Motor limit

"Motor switch-off limit"

The motor switch-off limit P534 [-01] has triggered.

Reduce load on motor

Set higher value in (P534 [-01]).

12.2

Generator limit

"Generator switch-off limit"

The generator switch-off limit P534 [-02] has triggered.

Reduce load on motor

Set higher value in (P534 [-02]).

12.5

Load limit

Switch-off due to overshooting or undershooting of
permissible load torques ((P525) … (P529)) for the time set
in (P528).

Adjust load.

Change limit values ((P525) ... (P527)).

Increase delay time (P528).

Change monitoring mode (P529).

12.8

Analog In minimum

Switch-off due to undershooting of the 0% adjustment value
(P402) with setting (P401) "0-10V with switch-off on error 1"
or "....2"

12.9

Analog In maximum

Switch-off due to overshooting of the 100% adjustment
value (P402) with setting (P401) "0-10V with switch-off on
error 1" or "....2"

Pos : 411 /Anleit ungen/6. / 7. Mel dungen z um Betriebsz ust and [BU 0500 / BU 0200]/ St örmel dungen/F ehl er E013 [ SK 180E ... SK 5xxE] @ 2\ mod_1347454271218_388.doc x @ 46751 @ @ 1

E013

13.0

Encoder error

No signal from encoder

Check 5V sensor if present.

Check supply voltage of encoder.

13.1

Speed slip error

"Speed slip error"

The slip speed error limit was reached.

Increase setting in P327.

13.2

Shut-down monitoring

The slip error monitoring has triggered; the motor could not
follow the setpoint.

Check motor data P201-P209! (Important for the
current controller)

Check motor circuit.

In servo mode, check the encoder setting P300 and
check the following

Increase setting value for torque limit in P112.

Increase setting value for current limit in P536.

Check deceleration time P103 and extend if
necessary

13.5

Reserved

Error message for POSICON

à see supplementary

instructions

13.6

Reserved

Error message for POSICON

à see supplementary

instructions

Pos : 412 /Anleit ungen/6. / 7. Mel dungen z um Betriebsz ust and [BU 0500 / BU 0200]/ St örmel dungen/F ehl er E014 "res er viert" [ SK 180E ... SK 5xxE] @ 2\ mod_1347454273854_388.doc x @ 46776 @ @ 1

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