Troubleshooting and diagnostics – LEESON SM4 Series Flux Vector User Manual

Page 66

Advertising
background image

65

Troubleshooting and Diagnostics

Fault

Cause

Remedy

(1)

f.HF

High DC Bus Voltage

fault

Mains voltage is too high

Check mains voltage and P107

Decel time is too short, or too

much regen from motor

Increase active decel time

(P105, P126, P127) or install

Dynamic Braking option

f.1L

Digital Input

Configuration fault

(P121...P123)

More than one digital input set for

the same function

Each setting can only be used

once (except settings 0 and 3)

Only one digital input configured

for MOP function (Up, Down)

One input must be set to MOP Up,

another must be set to MOP Down

PID mode is entered with setpoint

reference and feedback source

set to the same analog signal

Change PID setpoint reference

(P121…P123) or feedback source

(P201).

One of the digital inputs (P121…

P123) is set to 10 and another is

set to 11…14.

Reconfigure digital inputs

One of the digital inputs (P121…

P123) is set to 11 or 12 and

another is set to 13 or 14.
PID enabled in Vector Torque mode

(P200 = 1 or 2 and P300 = 5)

PID cannot be used in Vector

Torque mode

f.JF

Remote keypad fault

Remote keypad disconnected

Check remote keypad connections

f.LF

Low DC Bus Voltage fault Mains voltage too low

Check mains voltage

f.n1d

No Motor ID fault

An attempt was made to start the

drive in Vector or Enhanced V/

Hz mode prior to performing the

Motor Auto-calibration

See P300…P399 for Drive Mode

setup and calibration.

f.ntF

Module communication

fault

Communication failure between

drive and Network Module.

Check module connections

f.nF1

f.nF9

Network Faults

Refer to the module documentation.

for Causes and Remedies.

f.OF

Output fault:

Transistor fault

Output short circuit

Check motor/motor cable

Acceleration time too short

Increase P104, P125

Severe motor overload, due to:

• Mechanical problem

• Drive/motor too small for

application

• Check machine / system

• Verify drive/motor are proper

size for application

Boost values too high

Decrease P168, P169

Excessive capacitive charging

current of the motor cable

• Use shorter motor cables with

lower charging current

• Use low capacitance motor

cables

• Install reactor between motor

and drive.

Failed output transistor

Contact factory technical support

(1)

The drive can only be restarted if the error message has been resent.

Advertising
This manual is related to the following products: