Kawasaki D Series Controller MPVDCONTV113E-3 User Manual

Page 109

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TROUBLESHOOTING

D SERIES CONTROLLER

TROUBLESHOOTING AND COMPONENT REPLACEMENT

1-106

August 9, 2005

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ERROR CODE E1130

Jt XX collision was detected.

Motor current command value exceeds the threshold value set in AUX 0510.

Remove obstacles in the robot motion path area.

Ensure tool settings are correct.

If an obstacle was not encountered, increase the threshold value set in AUX 0510.

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ERROR CODE E1131

Jt XX Unexpected shock is detected.

Change in motor current command value, per unit of time, exceeds the threshold value
set in AUX 0510.

Remove obstacles in the robot motion path area.

Ensure tool settings are correct.

If an obstacle was not encountered, increase the threshold value set in AUX 0510.

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ERROR CODE E1132

Motor power OFF. Measurement stopped.

This error occurs when motor power is interrupted during auto load measurement.

Main causes include:
1. External HOLD/RUN switch is set to HOLD.
2. TEACH/REPEAT switch is set to TEACH.
3. External EMERGENCY STOP switch is pressed.

Reset switches to allow repeat operation. Repeat the auto load measurement.

Ensure the motor power is not interrupted during auto load measurement. Repeat
the auto load measurement.

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ERROR CODE E1133

Conveyor has reached max. value position.

The conveyor exceeded the maximum value set for the conveyor during program execu-
tion.

Ensure conveyor maximum value is set correctly.

Modify program data as necessary.

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