Rockwell Automation 7000L PowerFlex Medium Voltage AC Drive (C Frame) - Classic Control User Manual

Page 298

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Commissioning 4-93

7000 “C” Frame

7000L-UM300I-EN-P – Juen 2013


Reg in limit - indicates that the torque command was greater than
"Torque limit motoring" or "Torque limit braking". The measured
inertia value is invalid. Parameter "Autotune trq stp" or parameter
"Autotune spd cmd" must be set to a lower value and the test
repeated.


Tuning abort - indicates that the deviation in motor speed was
greater than 10 Hz. The measured inertia value is invalid.
Parameter "Autotune trq stp" must be set to a lower value and the
test repeated.


Inertia high - indicates that the measured total inertia is greater
than 5 seconds. This warning is intended to draw attention to an
unusually high inertia value. For a very high inertia load such as
a large fan, this may be a valid result and parameter "Total
inertia" should be manually set equal to "Autotune inertia".
However, a high inertia measurement could also be produced by
a value of "Autotune trq stp" which is too low.


Speed Regulator Manual Tuning


If it is not possible to tune the speed regulator using the autotune
function, then the step response of the speed regulator can be tuned
manually using the following procedure. To obtain accurate results,
the load torque must be steady.

1. Set parameter "Spdreg bandwidth” in "Speed Control" to 1.0

rad/sec.

Speed Control Parameter Screen


2. Set parameter "Total inertia" in "Speed Control" to an initial

value of 1.0 sec.

3. Assign parameter „Speed Error‟ in the "Current Control" group

to a SCBL test point (Rect TP1 or 2). This can be done similarly
to the way that the meter assignments were described earlier in
the chapter. Then it can be displayed on your oscilloscope. Use
the settings 2V/division and 1 sec/division.

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