Rockwell Automation 7000L PowerFlex Medium Voltage AC Drive (C Frame) - Classic Control User Manual

Page 501

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Troubleshooting

7-17

7000 “C” Frame

7000L-UM300I-EN-P – June 2013

FAULT

MESSAGE

FAULT

CODE

DESCRIPTION

RECOMMENDED ACTIONS

Motor Heartbeat

167

The DCB-L has detected the loss of the
heartbeat signal from the DCB-M.

– Verify DC Control voltages to both DCBs
– Possible Failed DCB – Check LED status

of both boards and compare with table in
the manual – Recycle power and replace

board if necessary

Motor Load Loss

74

The drive has detected a loss of load
condition. This is activated as a fault using
the parameter Load Loss Detect (P199),
and the necessary setpoints are Load Loss

Level (P246), Load Loss Delay (P231), and
Load Loss Speed (P259).

– Verify the parameter settings
– Ensure that the load should not normally

be in an unloaded condition

– This is designed for applications likely to

lose the load (downhole pump – hollow-

shaft motor) and we do not want to run
with the loss of load

Motor Neutral OV

67

The Neutral-to-Ground voltage measured
from the Output Filter Capacitor Neutral
point has exceeded Ground Fault

Overvoltage Trip (P189) for the duration set
in Ground Fault Overvoltage (P190). This
value is displayed in V Motor Neutral

(P347).

– Insulation Failure – Megger the motor

insulation/motor cables/drive insulation to
ground

– Verify the integrity of the output

grounding network if applicable

– Megger the input Isolation Transformer

Secondaries/Input Cables to ground

– Verify Parameter settings are appropriate

for AC Line Reactor or Isolation
Transformer drives

– Verify the integrity of Motor Filter

Capacitors, looking for short circuits or

signs of physical damage. Refer to
Chapter 6 of the User‟s Manual for
detailed instructions on Testing Filter

Capacitors.

Motor OC

21

The measured motor current I Stator (P340)
has exceeded Motor Overcurrent Trip
(P177) for the duration set in Motor

Overcurrent Delay (P178).

Possible Causes:
– Real OC/Transients
– Bad Burden resistor/Current Sensor

Circuit Failure – Check components

– Parameter settings too low compared to

torque limit – Verify Parameter settings

– Current regulator in limit (check line

voltage and Alpha line while running)

Motor OL

65

A Motor Overload condition has been
detected, where the overload condition is
calculated using I Stator(P340) and an
algorithm based on Motor Overload Trip
(P179) as the absolute trip level, Motor
Overload Delay (P180) as the base trip delay,

and Motor Overload Min (P351) as the point
where the overload calculation begins.

– Transient Loading - Check torque limit

and overload settings and Compare
loading to torque settings and trip
settings

– Burden Resistor – Check LEM feedback

and Check the burden resistors

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