Custom motor file, Troubleshooting custom motor files – Rockwell Automation 1398-DDM-xxx USE MNL/ULTRA 200 DIG.SERVO.DR User Manual

Page 280

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Publication 1398-5.0 – October 1998

D-16

Creating Custom Motor Files

Custom Motor File

The custom motor file parameters are as follows:

Troubleshooting Custom
Motor Files

GENERAL

CURRENT LOOP

Motor Model:

A_CUSTOM

Current Feedforward:

0 degrees / kRPM

Table ID:

-1

Motor File:

CUSTOM21.MTR

ELECTRICAL

Motor Type:

Synchronous

Resistance:

7.4 Ohms

Number of Poles:

8

Inductance:

10.0 mH

Kt:

0.61 N-m/Amp

Jm:

2.26 kg-cm

2

RATINGS

Ke:

44.0 Volts/kRPM

Continuous Torque:

1.4 Amps

Peak Torque:

3.8 Amps

Thermal Time Constant:

Checked, 1800 sec

FEEDBACK

Integral Thermostat:

Unchecked

Linecount:

1500 lines/rev

Maximum Speed:

4000 RPM

Index Offset:

0 degrees

Hall Offset:

120 degrees

Startup Commutation:

Hall / Hall

Invert Direction:

Unchecked

Problem

Possible Causes

Motor locks at a certain location.

Motor jumps once at startup.

Motor runs away.

Low torque production.

1.Motor phasing is incorrect.

2.Hall Offset is incorrect.

3.Incorrect startup commutation.

4.Incorrect encoder phasing.

5.Incorrect pole count.

6.Incorrect encoder linecount.

High audible noise from motor.

Velocity loop difficult to stabilize.

Shaft vibration.

1.Incorrect motor resistance.

2.Incorrect motor inductance.

3.Inductance too low.

4.Electrical time constant too low.

5.Low encoder linecount.

Underdamped velocity response.

Overdamped velocity response.

1.Incorrect motor inertia.

2.Incorrect torque constant.

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