Yaskawa iQpump Controller User Manual User Manual

Page 141

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6.1 Fault Detection

YASKAWA TM.iQp.06 iQpump Controller User Manual

141

oL2

Inv Overloaded

iQpump Overload

Designed to protect the iQpump.

The load is too large. The cycle

time is too short at the accel / decel

time.

Recheck the cycle time and the size of

the load as well as the times set in C1-01

and C1-03 to C1-06.

The voltage of the V/f pattern is

high.

Review the V/f pattern parameters, E1-

01 thru E1-13.

The size of the iQpump is small.

Change to a larger size iQpump.

oL3

Overtorque Det 1

Overtorque Detection 1

iQpump output current > L6-02 for more than the

time set in L6-03.

Motor is overloaded.

Ensure the values in L6-02 and L6-03

are appropriate.
Check application / machine status to
eliminate fault.

oPR

Oper Disconnect

Digital Operator Connection Fault

The iQpump will stop if the digital operator is

removed when the iQpump is commanded to run
through the digital operator.

The digital operator is not attached
or the digital operator connector is

broken.

Attach the digital operator.
Check the digital operator connector.

Verify the setting of o2-06.

oV

DC Bus Overvolt

DC Bus Overvoltage

208-240 Vac: Trip point is

≥ 400 Vdc.

480 Vac: Trip point is

≥ 800 Vdc.

High input voltage at R/L1, S/L2

and T/L3.

Check the input circuit and reduce the.

input power to within specifications

The deceleration time is set too

short.

Extend the time in C1-02, C1-04 or C1-

06.

Power factor correction capacitors
are being used on the input to the

iQpump.

Remove the power factor correction

capacitors.

PF

Input Pha Loss

Input Phase Loss

iQpump input power supply has an open phase or

has a large imbalance of input voltage.

Open phase on input of the
iQpump.

Check the input voltage.

Loose terminal screws at R/L1,

S/L2 or T/L3.

Tighten the terminal screws.

Momentary power loss occurred.

Check the input voltage.

Input voltage fluctuation too large. Check the input voltage.

Parameter L8-06 value is set

incorrectly.

Verify parameter L8-06 is set
correctly per the kVA tables on pages C-

2 and C-3. Adjust L8-06 according to

your application. The higher the value
the less sensitive it becomes.

CAUTION: Changing this parameter

from the factory default setting may

cause iQpump failure and void the
product warranty. (Consult the

factory for application assistance).

PUF

DC Bus Fuse Open

DC Bus Fuse

Detects if the DC bus fuse has opened.

Shorted output transistor(s) or

terminals.

Remove power from the iQpump.
Disconnect the motor.
Perform the checks without power in

Table 6.6.
Replace the shorted component(s).
Replace the defective fuse.

rH

DynBrk Resistor

Dynamic Braking Resistor

The protection of the dynamic braking resistor

based on setting of L8-01.

Overhauling load, extended
dynamic braking duty cycle,

defective dynamic braking resistor.

Verify dynamic braking duty cycle.
Monitor DC bus voltage.
Replace dynamic braking resistor.

rr

DynBrk Transistr

Dynamic Braking Transistor

The dynamic braking transistor failed.

Shorted dynamic braking

transistor, high DC bus voltage,
defective dynamic braking resistor.

Cycle power off and on to the iQpump.
Replace defective dynamic braking

transistor or resistor.
Monitor DC bus voltage.

Uv1

DC Bus Undervolt

DC Bus Undervoltage

The DC bus voltage is

≤ L2-05.

208-240 Vac: Trip point is

≤ 190 Vdc.

480 Vac: Trip point is

≤ 380 Vdc.

Low input voltage at R/L1, S/L2

and T/L3.

Check the input circuit and increase the

input power to within specifications.

The acceleration time is set too
short.

Extend the time in C1-01, C1-03, or C1-
05.

Voltage fluctuation of the input

power is too large.

Check the input voltage.

Digital

Operator Display

Description

Cause

Corrective Action

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