Yaskawa iQpump Micro User Manual

Page 170

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Digital Operator Display

Fault Name

The feedback signal has risen above the

level set in P1-11, High Feedback Level,

for the time set in P1-12, High Feedback

Level Fault Delay Time.

This is effective only when P1-13, High

Feedback Selection, is set to 0 (Fault and

digital out).

• Set the High Feedback fault characteristics in P1-11 and P1-12.
• Drive response to this condition is controlled by P1-13, High Feedback Selection. Auto-restart of this fault

is controlled by L5-41, High Feedback Fault Retry Selection.

Digital Operator Display

Fault Name

HWL

(HIH20)

High Water Level
The “High Water Level” digital input is active (H1-0o = 90).

Cause

Possible Solution

The Low Water Level switch is activated or

P1-31, High Water Digital Input

Configuration, is programmed incorrectly.

Lower the water level and/or adjust the High Water Level switch.

Digital Operator Display

Fault Name

LF

Output Phase Loss
• Phase loss on the output side of the drive.
• Setting L8-07 to 1 or 2 enables Phase Loss Detection.

Cause

Possible Solution

The output cable is disconnected

• Check for wiring errors and properly connect the output cable.
• Correct the wiring.

The motor winding is damaged

• Check the resistance between motor lines.
• Replace the motor if the winding is damaged.

The output terminal is loose

Apply the tightening torque specified in this manual to fasten the terminals.

Refer to Wire Gauges and

Tightening Torques on page 70

for details.

The rated current of the motor being used

is less than 5% of the drive rated current

Check the drive and motor capacities.

An output transistor is damaged

If the problem continues, replace the drive.

A single-phase motor is being used

The drive cannot operate a single phase motor.

Digital Operator Display

Fault Name

LF2

Output current imbalance
One or more of the phases in the output current is lost.

Cause

Possible Solution

Phase loss has occurred on the output side

of the drive.

• Check for faulty wiring or poor connections on the output side of the drive.
• Correct the wiring.

Terminal wires on the output side of the

drive are loose.

Apply the tightening torque specified in this manual to fasten the terminals.

Refer to Wire Size and Torque

Specifications on page 77

for details.

No signal displays from the gate driver

board.

Replace the drive. Contact Yaskawa for assistance.

Motor impedance or motor phases are

uneven.

• Measure the line-to-line resistance for each motor phase. Ensure all values are the same.
• Replace the motor. Contact Yaskawa for assistance.

Digital Operator Display

Fault Name

LFB

Low Feedback
The feedback signal is too low.

Cause

Possible Solution

The feedback signal has dropped below the

level set in P1-08, Low Feedback Level, for

the time set in P1-09, Low Feedback Level

Fault Delay Time.

This is effective only when P1-10, Low

Feedback Selection, is set to 0 (Fault and

digital out).

• Set the Low Feedback fault characteristics in P1-08 and P1-09.
• Drive response to this condition is controlled by P1-10, Low Feedback Selection.
• Auto-restart of this fault is controlled by L5-40, Low Feedback Fault Retry Selection.

5.2 Fault Detection

170

YASKAWA TOEP YAIQPM 03B YASKAWA AC Drive - iQpump Micro User Manual

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