Rockwell Automation FlexPak 3000 Digital DC Drive Version 4.3 User Manual

Page 134

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13-2

FlexPak 3000 DC Drive Software Reference

F00002

TACHOMETER

LOSS

Tachometer or encoder feedback signal missing.

Possible causes:

Tachometer or encoder coupling failure.

Disconnected, loosely connected, or damaged tachometer or encoder
wires.

Pulse encoder supply voltage low.

Incorrect analog tachometer scaling.

Incorrect pulse encoder configuration.

Motor armature winding not connected or open circuit.

Blown inverting fault (DC) fuse.

Inverting fault breaker tripped.

High inertia loads and high inductance armature circuits. To reduce
nuisance faults, increase the firing angle threshold (see section 13.2).

Tachometer or encoder failure.

F00003

OVERSPEED

Motor speed exceeded the 110% of

TOP

SPEED

.

Possible causes:

Incorrect tachometer or encoder scaling.

Blown field supply fuse(s).

Improper speed loop tuning.

PULSE

TACH

QUADRATURE

set to

ON

for a non-regenerative drive.

Incorrect pulse encoder wiring.

F00004

FIELD

CURRENT

LOSS

Standard or enhanced field supplies: The field loss detection circuit does
not sense any field current flowing in the motor shunt field.

Field Current Regulator kit field supply:

FIELD

FEEDBACK

(P.589) fell below

the

FIELD

LOSS

THRESHOLD

(P.512).

Possible causes:

Motor field winding not connected or open circuit.

Blown field supply fuse(s).

Blown AC line fuse(s).

Field supply failure.

Disconnected, loosely connected, or damaged wiring harness.

Field Current Regulator kit only: Improper field loop tuning.

Table 13.1 – Fault Codes (Continued)

Code

OIM Display

Description

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