Yaskawa VS-626 MC5 User Manual

Page 124

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6.2

Open-loop Vector Control

- 21

6.2.3 Autotuning Faults

D

One of the fault messages in the following table will be displayed if a fault occurs during autotuning
and the motor will stop. In this case, determine the cause of the fault, correct it, and perform autotuning
again.

D

The fault display can be cleared by pressing the MENU Key.

D

The motor constants will revert to their default settings if a fault occurs. Set these constants again be-
fore starting autotuning again.

Table

6.2

Troubleshooting Autotuning Faults for Open-loop Vector Control

Fault Display

Probable Cause

Remedy

Data Invalid
(Motor data fault)

There was a fault in the data
set during autotuning.

There was a fault in the rela-
tionship between the rated
frequency, rated speed, and
number of poles.

Change the settings to conform to the follow-
ing equation:
Rated speed < 120

u Motor frequency/Num-

ber of poles

A load is connected to the
motor.

Remove the load.

ALARM: Over Load
(Excessive tuning load)

The effective load factor ex-
ceeded 20% during autotun-
ing

There was a setting fault dur-
ing autotuning.

Check the rated current setting. Change if
necessary.

(Excessive tuning load)

ing.

There is a motor bearing
problem.

Turn the Inverter off and rotate the motor by
hand.
Replace the motor if it doesn’t turn smoothly.

Motor speed

The torque reference value
exceeded 100% during auto

There is a broken/discon-
nected motor power wire.

Check and replace wiring components if nec-
essary.

Motor speed
(Motor speed fault)

exceeded 100% during auto-
tuning.

A load is connected to the
motor.

Remove the load.

The torque limit function is
operating.

Initialize the torque limit constants (H7-01 to
H7-04).

Accelerate
(Acceleration fault)

The motor doesn’t accelerate
within the prescribed time.

The acceleration time is too
short.

Increase acceleration time 1 (C1-01).

(Acceleration fault)

A load is connected to the
motor.

Remove the load.

Rated Slip
(Rated slip fault)

The rated slip setting can’t
be tuned within the pre-
scribed time.

A load is connected to the
motor.

Remove the load.

Saturation -1
(Iron core saturation coefficient
1 fault)

The core-saturation coeffi-
cients can’t be tuned within

The rated current setting isn’t
correct.

Check and change the setting if necessary.

Saturation -2
(Iron core saturation coefficient
2 fault)

cients can’t be tuned within
the prescribed time.

There is a broken/discon-
nected motor power wire.

Check and replace wiring components if nec-
essary.

Resistance
(Line-to-line resistance fault)

The motor terminal resist-
ance or no-load current set-

The rated current setting isn’t
correct.

Check and change the setting if necessary.

No-load Current
(No-load current fault)

ance or no-load current set-
ting can’t be tuned within the
prescribed time.

There is a broken/discon-
nected motor power wire.

Check and replace wiring components if nec-
essary.

Tune Aborted
Minor Fault:

---

A minor Inverter fault oc-
curred.

Check the minor fault indicated in the boxes
in the display shown at the left.

Tune Aborted
V/f Over Setting
(Displayed after the completion

Torque reference exceeded
100%, and no--load current

Rated voltage and rated fre-
quency settings are not cor-
rect.

Check the setting and correct any problems.

(Displayed after the completion
of autotuning)

100%, and no--load current
exceeded 70%.

The load is connected to the
motor.

Disconnect the motor from the load.

6

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