Rockwell Automation 2094-EN02D-M01-Sx Kinetix 6200 and Kinetix 6500 Modular Multi-axis Servo Drives User Manual User Manual

Page 203

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Rockwell Automation Publication 2094-UM002E-EN-P - May 2012

203

Troubleshooting the Kinetix 6200 and Kinetix 6500 Drive System

Chapter 8

FLT S61…ENABLE INPUT

Drive Enable Input

The hardware enable input was
deactivated while the drive was
enabled.

An attempt was made to
enable the axis through
software while the Drive
Enable hardware input was
inactive.

Disable the Drive Enable Input
fault.

The Drive Enable input
transitioned from active to
inactive while the axis was
enabled.

Verify that Drive Enable hardware
input is active whenever the drive
is enabled through software.

FLT S62…CONTROLLER
(Kinetix 6500 drives only)

Controller Initiated Exception

The controller has requested the drive
to generate an exception.

User configured software
overtravel

Move axis out of soft

overtravel range.

Clear soft overtravel fault.
Check soft overtravel

configuration.

Consult controller

documentation.

Table 81 - FLT Sxx Fault Codes (continued)

Four-character
Display Message

RSLogix 5000
Fault Message

Problem or Symptom

Potential Cause

Possible Resolution

Table 82 - FLT Mxx Fault Codes

Four-character
Display Message

RSLogix 5000
Fault Message

Problem or Symptom

Potential Cause

Possible Resolution

FLT M01…SELF SENSING

Self-sensing Startup Fault

The self-sensing commutation start-up
algorithm failed.

Extremely light or heavy
load on the motor.

Clear faults and re-try.

Mechanical obstruction.

Reduce friction.
Check for mechanical

obstruction.

FLT M02…MOTOR VOLTAGE

Motor Voltage Mismatch

Motor voltage incompatible with drive
voltage.

Check RSLogix 5000
software configuration.

Correct RSLogix 5000 software
configuration.

Wrong motor connected to
drive.

Connect appropriate motor to
drive.

FLT M04…MTR FDBK FILTER nn
(Kinetix 6500 drives only)

Motor Feedback Filter

Excessive levels of noise have been detected
by the digital feedback filter. The nn field is
defined as follows:

01: Sine or A channel
02: Cosine or B channel

The motor feedback wiring
is open, shorted, or missing.

Use shielded cables with

twisted pair wires.

Route the feedback away from

potential noise sources.

Check the system grounds.
Replace the motor/encoder.

FLT M04…AUX FDBK FILTER nn
(Kinetix 6500 drives only)

Aux Feedback Filter

The auxiliary feedback
wiring is open, shorted, or
missing.

FLT M05…MTR FDBK BATT LOSS

Motor Encoder Battery Loss

The battery voltage on a battery-
backed motor encoder is low enough
such that absolute position is no longer
available.

Weak battery or poor
battery connection.

Replace battery.
Check battery connection.

FLT M06…MTR FDBK BATT LOW

Motor Encoder Battery Caution

The battery voltage on a battery-
backed motor encoder is below a
caution level.

FLT M07…MTR INCR LOSS

Motor Incremental Position
Loss

The periodic check of the incremental
encoder position against the absolute
encoder position or Hall edges (when
available) indicates they are out of
tolerance.

The motor feedback wiring
is open, shorted, or missing.

Check motor encoder wiring.
Run Hookup test in

RSLogix 5000 software.

FLT M07…AUX INCR LOSS

Aux Incremental Position Loss

The auxiliary feedback
wiring is open, shorted, or
missing.

FLT M10…CTRL OVERTEMP FL

Control Module
Overtemperature

The control module temperature has
exceeded its limit.

Cabinet ambient
temperature has exceeded
50 °C (122 °F).

Reduce cabinet ambient
temperature.

FLT M11…CTRL OVERTEMP UL
(Kinetix 6500 drives only)

Control Module
Overtemperature

The control module temperature has exceeded a user limit.

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