Oc6: i2xt motor overload, Oc6: i2xt overload motor, Error message – Lenze 8400 HighLine User Manual

Page 655: Lp1: motor phase failure, Sd3: open circuit - feedback system, Xx.0123.00145, Xx.0123.00105, Xx.0123.00205, Xx.0123.00200, Xx.0123.00201

Advertising
background image

Lenze · 8400 HighLine · Referenzhandbuch · DMS 10.0 EN · 06/2014 · TD05/TD14

655

9

Diagnostics & error management

9.9

Error messages of the operating system

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

oC6: I2xt overload - motor [xx.0123.00105]

LP1: Motor phase failure [xx.0123.00145]

Sd10: Speed limit - feedback system 12 [xx.0123.00200]

Sd11: Speed limit for feedback system 67 [xx.0123.00201]

Sd3: Open circuit - feedback system [xx.0123.00205]

Response (Lenze setting printed in bold)

Setting:

C00606

( Adjustable response)

0: No Reaction  1: Fault  2: Trouble  3: TroubleQuickStop  4: WarningLocked  5: Warning  6: Information

Cause

Remedy

Thermal overload of the motor.

Only self-ventilated motors can be monitored using the

I2xt function.

• Check whether is it a self-ventilated motor. If not, set

C00606

to "0: No Reaction".

• Observe load requirements.

• Correct dimensioning if necessary.

• For VFCplus control type: Check Vmin boost (

C00016

).

Set Vmin boost

Response (Lenze setting printed in bold)

Setting:

C00597

( Adjustable response)

0: No Reaction  1: Fault  2: Trouble  3: TroubleQuickStop  4: WarningLocked  5: Warning  6: Information

Cause

Remedy

Motor phase failure - power section

• This error message is displayed if a motor phase

carries less current of one half-wave than set in

C00599

.

• Check the motor connections and the corresponding

plug connector on the device and, if necessary, the

motor terminal box.

• Check the trigger threshold (

C00599

).

Response (Lenze setting printed in bold)

Setting:

C00607

( Adjustable response)

0: No Reaction  1: Fault  2: Trouble  3: TroubleQuickStop  4: WarningLocked  5: Warning  6: Information

Cause

Remedy

Maximally permissible speed of the feedback system

connected to DI1/DI2 reached.

Reduce speed of the rotation shaft/feedback system.

n

encoder

<= (f

max

x 60) / encoder increments

(for f

max

= 10 kHz)

Response (Lenze setting printed in bold)

Setting:

C00607

( Adjustable response)

0: No Reaction  1: Fault  2: Trouble  3: TroubleQuickStop  4: WarningLocked  5: Warning  6: Information

Cause

Remedy

Maximally permissible speed of the feedback system

connected to DI6/DI7 reached.

Reduce speed of the rotation shaft/feedback system.

n

encoder

<= (f

max

x 60) / encoder increments

(for f

max

= 10 kHz)

Response (Lenze setting printed in bold)

Setting:

C00586

( Adjustable response)

0: No Reaction  1: Fault  2: Trouble  3: TroubleQuickStop  4: WarningLocked  5: Warning  6: Information

Cause

Remedy

• HTL encoder cable interrupted.

• HTL encoder is defective.

Note: The reason can also be a very dynamic acceleration

or an approach against a blocked motor shaft, e.g. with a

a closed holding brake or when referencing to positive

stop (mode 14/15) and a waiting time (

C01223

)

>100 ms.

• Check HTL encoder cable.

• Check HTL encoder.

• Check related terminals.

• Switch off monitoring (

C00586

= "0: No reaction")

when the HTL encoder is not used.

Advertising