A.40 – Yaskawa DR2 Sigma Servo User Manual

Page 407

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6.2 Troubleshooting

395

Status When Alarm Occurred

A

During servomotor

operation

Overflow during

high-speed opera-

tion

No feedback pulse

returned after refer-

ence pulse input.

Normal operation

but overflow when

large reference in-

put.

At control power ON

B

,

F

C

,

D

,

E

F

Cause

Remedy

A

Servomotor wiring incorrect.

Check and correct wiring. (Check A-, B-,

C h

l

2CN )

B

Encoder wiring incorrect (disconnection,

short, power supply, etc.)

g (

,

,

C-phase pulses correct at 2CN.)

C

Servopack adjustment incorrect

Increase speed loop gain (Cn-04) and/or

position loop gain (Cn-1A).

D

Servomotor overloaded

Reduce load torque and inertia. Otherwise,

replace with larger capacity servomotor.

E

Position reference pulse frequency too

high

• Decrease reference pulse frequency.
• Use smoothing function.
• Change electronic gear ratio.

F

Circuit board (1PWB) defective.

Replace Servopack.

D

Display and Outputs

Digital Operator

Di l

d

Alarm Output

g

p

Display and

Alarm Name

Alarm Code Output

Alarm Output

Alarm Name

ALO1

ALO2

ALO3

p

A.40

Overvoltage

OFF

OFF

ON

OFF

OFF: Output transistor is OFF
ON: Output transistor is ON

Status When Alarm Occurred

A

, D

During servomotor

operation

During motor

deceleration

During normal

operation

At main circuit power ON

B

,

C

, D

E

At control power ON

F

6

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